摘要
针对大同发电有限责任公司2台600 MW机组主汽压力和负荷相互适应能力差、协调不稳定、投入发电机自动控制系统(AGC)后负荷升降速度慢等问题,制定了相应的优化措施,使机组对负荷指令的响应速度大大提高,保证了AGC投入的可靠性。
In the light of low adaptability between main steam pressure load,unstable coordination in Datong Power Generation Corp.Ltd.with capacity of 2×600MW,considering the low speed of load increasing or decreasing after the commissioning of AGC system,the related optimal measures are set up to speed up the response to load command,and ensure the reliability of the commissioning of AGC.
出处
《陕西电力》
2010年第3期46-48,共3页
Shanxi Electric Power