摘要
分析全钢载重子午线轮胎胎圈气泡的产生原因并提出相应改进措施。施工设计及半成品尺寸不当、排气线完整性差、成型贴合压辊位置不合理及硫化模具钢圈排气线不通等均会导致胎圈气泡缺陷。经过优化施工设计、增加胎侧及加强层刺孔工艺、规范半成品尺寸过渡及成型辊压等措施能够有效减少胎圈气泡的产生,提高轮胎合格率。
The causes of bead bubbles of truck and bus radial tire were analyzed and corresponding improvement measures were put forward.Improper construction design and semi-finished product size,poor integrity of the exhaust line,unreasonable position of the building and laminating rollers,and unreasonable exhaust line of the steel ring of curing mold all led to the defect of bead bubbles.By optimizing the construction design,increasing the puncture process of the sidewall and reinforcement layer,standardizing the size transition of semi-finished products and the rolling process of the tire building,the defects of bead bubbles could be effectively reduced,and the qualification rate of finished tire could be improved.
作者
初坤龙
周君兰
吕伟
孙宗涛
张彦军
CHU Kunlong;ZHOU Junlan;LYU Wei;SUN Zongtao;ZHANG Yanjun(Prinx Chengshan(Shandong)Tire Co.,Ltd,Rongcheng 264300,China)
出处
《轮胎工业》
CAS
2022年第6期369-372,共4页
Tire Industry
关键词
全钢载重子午线轮胎
胎圈气泡
排气线
成型辊压
半成品尺寸
truck and bus radial tire
bead bubble
exhaust line
building roller
size of semi-finished product