摘要
针对某厂DMS森吉米尔轧机生产无取向硅钢表面麻面缺陷的问题,根据生产实际,对其形成原因从乳化液及工作辊两方面因素进行了分析。结果表明:乳化液对麻面缺陷的产生有一定影响,但不是主要因素,主要原因是由于二十辊森吉米尔轧机工作辊辊径较小,轧制相同长度带钢轧辊运转周期较大,容易产生疲劳失效而导致。为此,提出通过调整冷轧工序成品轧制道次的压下率以减小轧制力,从而减小工作辊的磨损疲劳;通过对轧制乳化液浓度、温度的合理控制,以改善润滑效果、提高轧制速度,而进一步缓解轧辊疲劳的改进措施,使该钢厂无取向硅钢麻面缺陷发生率由原来的18%降至0.8%,带钢表面质量明显改善。
For the problem of surface pockmarks of non-oriented silicon steel strip produced by a DMS Sendzimir mill, based on the production practice, the formation causes were analyzed from two aspects of emulsion and working roll. The results show that the emulsion has a certain effect on the formation of surface pockmarks defects, but it is not the main factor. The main reason is that the working roll diameter of the 20-high Sendzimir mill is small, and the running period of the roll rolling the same length is large, which is easy to produce fatigue failure. Therefore, it is put forward that the rolling force can be reduced by adjusting the reduction ratio of the finished products in the cold rolling process to reduce the wear and fatigue of the work roll, and by controlling the concentration and temperature of the rolling emulsion reasonably to improve the lubrication effect, increase the rolling speed and further alleviate the roll fatigue. The occurrence rate of surface pockmarks defects of non-oriented silicon steel strip was reduced from 18% to 0.8%, and the surface quality of strip was improved obviously.
作者
钟路
刘小东
ZHONG Lu;LIU Xiaodong(Wuhan Research Institute of Materials Protection,Wuhan 430030,China)
出处
《轧钢》
2022年第1期101-105,共5页
Steel Rolling
关键词
无取向硅钢
麻面缺陷
乳化液
工作辊
摩擦磨损
疲劳
non-oriented silicon steel
surface pockmarks defects
emulsion
work roll
friction wear
fatigue