摘要
为研究夯土民居裂缝注浆修补技术的加固效果,采用两个基本一致的足尺1:1夯土结构模型进行模拟地震振动台试验。对两模型在各烈度地震下的地震反应进行对比,试验得出加固模型的开裂表现、加速度反应及层间位移角等均显著改善。验证了裂缝注浆修补技术对夯土结构加固的可行性,为夯土民居的加固改造提供参考和建议。
In order to study the reinforcement effect of grouting repair technology for bauxite cracks,two identical full-scale 1∶1 bauxite structure models are applied to simulate seismic shaking table test.The seismic responses of the two models under various seismic earthquakes are compared.The results show that the cracking performance,acceleration response and interlayer displacement angle of the reinforcement model are significantly improved,and the feasibility of crack grouting repair technology for the reinforcement of bauxite structure is verified,and it provides the reference and suggestion for the reinforcement and reconstruction of bauxite dwellings.
作者
刘洪义
白羽
赖正聪
和磊
柏文峰
Liu Hong-yi;Bai Yu;Lai Zheng-cong;He Lei;Bai Wen-feng(School of Architectural Engineering,Kunming University of Science and Technology,Kunming 650500,China;School of Architecture and Urban Planning,Kunming University of Science and Technology,Kunming 650500,China)
出处
《工程抗震与加固改造》
北大核心
2020年第1期120-125,共6页
Earthquake Resistant Engineering and Retrofitting
基金
国家自然科学资助项目(51368027).
关键词
夯土民居
裂缝注浆加固
振动台试验
抗震性能
bauxite dwellings
crackgrouting reinforcement
shaking table tests
seismic performance