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泵站出水池-无压隧洞过渡段体型优化研究

Optimization of transition section shape from outlet sump of pumping station to free-flow tunnel
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摘要 泵站出水池到无压隧洞过渡段体型对隧洞的过流能力、沿程水面线及局部水头损失影响显著。针对某泵站工程过渡段的水流特性问题,采用比尺为1∶25物理模型对该过渡段进行了优化研究,延长了过渡段长度,增加了边墙扭曲段。研究发现:模型改进后,过流能力增加,水流平稳;局部水头系数从原设计的0.057~0.111减小至0.051~0.111;中心线水面线的纵向变化幅度减小。通过各项指标表明,优化后的过渡段比原设计方案显现出更为优良的特性,提出的优化设计方法可为其他类似工程提供借鉴经验。 The influence of transition section shape from outlet sump of pumping station to free-flow tunnel on current capacity,surface line and local head loss is significant.Aiming at solving the problem that the flow characteristic of a pump station is complex,the transition section was lengthened and warped surface wall was optimized by a test model with a geometric scale of 1/25 in accord with.The results show more smooth streamlines and an increase in flow capacity in the modified transition,along with a reduction from 0.051~0.074 to 0.051~0.074 in local head loss and a reduction in ranges of central longitudinal water surface profiles.The hydraulic characteristics indicators show that the transition section after optimization performs a better characteristics compared with that of the original design scheme.The optimal design of the project can provide a reference for other similar projects.
作者 王月华 王斌 吴德忠 韩晓维 张鸿清 王自明 WANG Yuehua;WANG Bin;WU Dezhong;HAN Xiaowei;ZHANG Hongqing;WANG Ziming(Zhejiang Institute of Hydraulics and Estuary,Hangzhou 310020,China;Yuyao Water Resources Bureau,Yuyao 315400,China)
出处 《水资源与水工程学报》 CSCD 2018年第4期138-142,共5页 Journal of Water Resources and Water Engineering
基金 浙江省科技计划项目(2017F30013) 浙江省水利科技计划项目(RC1603)
关键词 泵站出水池 无压隧洞 过渡段 体型优化 模型试验 outlet sump of pumping station free - flow tunnel transition section shape optimization model test
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