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RSM3/3多轴向经编机的动平衡研究 被引量:3

Study on Dynamic Balance of RSM3/3 Multiaxial Warp Knitting Machine
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摘要 为了降低RSM3/3多轴向经编机的振动,提高设备的运行速度,对RSM3/3多轴向经编机的成圈机构进行配重前后的动平衡分析。利用Solidworks软件搭建三维模型,并分析现有各个成圈机构的质心运动情况,通过添加配重块,改变各个机构的质心运动范围,得到机构配重块的最佳外径,并通过试验进行验证。经试机检测表明,在相同的运行条件下,RSM3/3多轴向经编机的曲轴配重后,设备的振动与噪音均有所降低,对多轴向经编机的设计具有一定的借鉴意义。 In order to reduce the vibration of RSM3/3 muhiaxial warp knitting machine and improve the running speed of the equipmenl, the dynamic, balance of RSM3/3 muhiaxial warp knitting machine knitting device befi^re and after applying counterweight was analyzed. The three-dimensional model was buih by using Solidworks software, and the movements of' center of' mass motion of all the existing knitting deviees were analyzed. The motion range of the center of mass of each mechanism was changed by adding the counterweight block, and the optimum outer diameter of the counterweight block was obtained, which was verified by experiments. The testing resuhs show that under the same operation conditions, the vibration and noise of the RSM3/3 muhiaxial warp knitting machine ate redueed after the weight is laid on the crankshaft, which has certain reference significance for the design of the nmltiaxial warp knitting machine.
作者 赵加洋 曹清林 赵红霞 张大伟 丁伟 Zhao Jiayang1, Cao Qinglin2, Zhao Hongxia1, Zhang Dawei1, Ding Wei(1.Jiangsu Runyuan Hohting Group Co., 1.td., Changzhou, Jiangsu 213131, China; 2.School of Mechanical Engineering, Jiangsu University of Technology, Changzhou, Jiangsu 213001, Chin)
出处 《针织工业》 北大核心 2018年第3期25-28,共4页 Knitting Industries
关键词 RSM3/3多轴向经编机 动平衡 成圈机构 曲轴 Solidwoks建模 RSM3/3 Muhiaxiai Warp Knitting Machine Dynamic Balance Knitting Device Crankshaft Solidworks Modeling
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