摘要
丁辛醇装置缩合系统在反应过程中排出一部分含碱废水,其中COD大于40000 mg/L,经多效蒸发及汽提系统处理后的废水COD小于500 mg/L,可回收部分有机物,既有较好的经济效益,又减轻了下游污水处理压力。
Part of alkaline wastewater is discharged in the condensation system of butyl octanol unit. The wastewater COD can be reduced to less than 500 mg,/L from more than 40 000 mg/L through multi - effect evaporation and stripping process. Meanwhile, part of organic phase earl be recovered, which is good to economic benefit and downstream wastewater treatment.
出处
《齐鲁石油化工》
2011年第3期202-204,共3页
Qilu Petrochemical Technology
关键词
含碱废水
多效蒸发
汽提
丁辛醇
COD
alkaline wastewater
multi - effect evaporation
stripping
butyl octanol
COD