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文留油田高含水期高效调整井设计 被引量:1

The Design of High-effect Adjustment Well in High Water Cut Stage about Wenliu Oilfield
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摘要 文留油田为复杂断块油田,已进入高含水期开发阶段,通过不断加深油藏微构造、沉积微相研究和剩余油分布规律研究,寻找剩余油富集区,并在经济评价的基础上设计调整井,打出了一批高效调整井,减缓了油田产量递减,改善了油田开发效果。 As a complex block-fault oilfield,Wenliu oilfield has developed into high water cut stage. By continually deepening the research of the micro-structure, sedimentary micro-phase and remaining oil distribution about the oilfield, we found out remaining oil enriched block. Based on the economic estimating, we designed high-effect adjusting well. The technology reduced the decline of production about the oilfield, achieved better developing effect.
出处 《断块油气田》 CAS 1999年第3期49-51,共3页 Fault-Block Oil & Gas Field
关键词 油藏地质 剩余油 调整井 高含水期 油田开发 Wenliu oilfield, Reservoir geology, Remaining oil, Adjusting well
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