摘要
介绍中国石化青岛炼油化工有限责任公司加氢处理装置的设计能耗与标定能耗,分析装置标定能耗降低的影响因素。根据装置的运行情况,提出了在一台往复压缩机上装备Hydrocom气量无级调节控制系统、用0.45MPa蒸汽替代1.0MPa蒸汽进行伴热和高压贫胺液增压泵改造三项节能技术改造措施,并从理论上分析与探讨了节能改造的可行性。
The design energy consumption and actual energy consumption of the hydrotreating unit of Qingdao Refining & Chemical Company were introduced, and the causes of lower energy consumption in performance test were analyzed. Based on the operation status of this unit, three measures for further energysaving were proposed including adding Hydrocom step less control system on one reciprocating compressor, using 0.45 MPa steam instead of 1.0 MPa steam for heating and revamping the amine depleted high pressure booster pump to meet the required operation parameters. The feasibility and predicted energy-saving results of adopting these three revamping measures were discussed.
出处
《石油炼制与化工》
CAS
CSCD
北大核心
2010年第1期72-76,共5页
Petroleum Processing and Petrochemicals
关键词
加氢处理
能耗
节能
技术改造
hydrotreating
energy consumption
energy conservation
technical transform