摘要
为减少轴承钢300 mm×300 mm连铸坯的碳偏析,通过CFX-4.4软件仿真分析了连铸结晶器内钢水流动和传热凝固过程,探讨了有关工艺参数和浸入式水口结构的关系。实践表明,通过4孔水口替代直孔水口,铸坯的碳偏析级别由1.0~2.0级降至1.0~1.5级,采用4孔水口中心碳偏析≤1.0级占79%,直孔水口仅为50%。
Liquid steel flow and heat transfer-solidification process were simulated and analyzed by CFX-4.4 software, and relation between relative process parameters and immersed nozzle structure has been discussed in order to decrease carbon segregation of 300 mm x 300 mm cast bloom of bearing steel. Production practice showed that a immersed nozzle with 4 holes was used instead of original one with straight hole, the center carbon segregation rating of cast bloom decreased from 1.0 - 2. 0 to 1.0 - 1.5, and the percentage of ≤ 1.0 rating of bloom with using 4 holes nozzle was 79% while that with using straight hole nozzle was only 50%.
出处
《特殊钢》
北大核心
2009年第3期46-47,共2页
Special Steel
关键词
轴承钢
连铸方坯
4孔浸入式水口
中心碳偏析
Bearing Steel, Cast Bloom, Immersed Nozzle with 4 Holes, Center Carbon Segregation