摘要
通过低周反复加载试验对3个内隔板一面贯通式节点进行了试验研究,研究了不同轴压比情况下节点的滞回性能、强度及刚度退化、延性、耗能性能及破坏特征。试验结果表明,试件的层间位移延性系数为2.11~2.32,峰值荷载时的能量耗散系数为1.141~1.502。提出了抗震设计、研究建议。
A total of three experimental specimens of penetrated interior diaphragm on one side had been tested under low-cyclic reversed loading to study the hysteric behavior, strength and stiffness degradation, ductility, energy dissipation capacity and the failure modes. The only difference of all specimens was the axial compression ratio. Experimental results show that the story drift ductility ratios are 2.11~2.32, and the energy dissipation ratios are 1. 141~1. 502 at the peak load. Additional anti-seismic design and research recommendations are presented.
出处
《重庆建筑大学学报》
EI
CSCD
北大核心
2007年第2期73-77,共5页
Journal of Chongqing Jianzhu University
关键词
方钢管混凝土柱
梁柱节点
内隔板贯通
试验研究
抗震性能
concrete-filled steel square tubular column
beam-to-column connection
through interior diaphragm
experimental study
seismic behavior