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打桩引起的基坑开挖问题及处理 被引量:3

Excavation problems induced by pile driving and their treatment
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摘要 通过某电厂桩基处理工程实例,介绍了打桩引起的预制桩偏位及开挖问题。在不加外荷载情况下,采用塑料排水板方法消散打桩引起的超静孔隙水压力的处理措施,解决了高孔隙水压力下主厂房的开挖问题。分析了塑料排水板消散孔隙水压力的影响因素。观测结果及工程实践表明,塑料排水板处理桩基工程快速经济,可不需加载,但处理效果与水平排水系统有关。 The deflection of precast piles and excavation problems induced by pile driving are introduced through an engineering case of pile foundation treatment of a power plant. The treatment and effectiveness by use of prefabricated drains method to dissipate the excess pore pressure by pile driving are also introduced under the condition without external loads. The excavation problems of the main power house under high pore pressure is solved; and factors related with prefabricated drains to dissipate pore pressure are analyzed. The observed results and engineering practice show that the pile foundation treatment by use of prefabricated drains is fast and economic; and it employs no external loads, however, the treatment effectiveness relates with the horizontal drainage system.
出处 《岩土力学》 EI CAS CSCD 北大核心 2006年第12期2246-2249,共4页 Rock and Soil Mechanics
关键词 桩基处理 超静孔隙水压力 预制桩 塑料排水板 开挖 pile foundation treatment excess pore pressure precast pile prefabricated drains excavation
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参考文献5

  • 1胡中雄编著..土力学与环境土工学[M].上海:同济大学出版社,1997:459.
  • 2CTAG02-97,塑料排水带地基设计规程[S]. 被引量:3
  • 3地基处理手册编写委员会.地基处理手册(第二版)[M].北京:中国建筑工业出版社,2000.. 被引量:50
  • 4焦志斌,李景林,吴春勇.池州电厂一期工程地基处理监测报告(土0062)[R].南京:南京水利科学研究院,2004. 被引量:2
  • 5徐永福,傅德明.结构性软土中打桩引起的超孔隙水压力[J].岩土力学,2000,21(1):53-55. 被引量:35

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