A current-mode buck DC-DC controller based on adaptive on-time (AOT) control is presented. The on-time is obtained by the techniques of input feedforward and output feedback, and the adaptive control is achieved by ...A current-mode buck DC-DC controller based on adaptive on-time (AOT) control is presented. The on-time is obtained by the techniques of input feedforward and output feedback, and the adaptive control is achieved by a sample-hold and time-ahead circuit. The AOT current-mode control scheme not only obtains excellent transient response speed, but also achieves the independence of loop stability on output capacitor ESR. In addition, the AOT current-mode control does not have subharmonic oscillation phenomenon seen in fixed frequency peak current-mode control, so there is no need of the slope compensation circuit. The auto-skip pulse frequency modulation (PFM) mode improves the conversion efficiency of light load effectively. The controller has been fabricated with UMC 0.6-μm BCD process successfully and the detailed experimental results are shown.展开更多
A 1500 mA,10 MHz self-adaptive on-time (SOT) controlled buck DC-DC converter is presented. Both a low-cost ripple compensation scheme (RCS) and a self-adaptive on-time generator (SAOTG) are proposed to solve the...A 1500 mA,10 MHz self-adaptive on-time (SOT) controlled buck DC-DC converter is presented. Both a low-cost ripple compensation scheme (RCS) and a self-adaptive on-time generator (SAOTG) are proposed to solve the system stability and frequency variation problem. Meanwhile a self-adaptive power transistor sizing (SAPTS) technique is used to optimize the efficiency especially with a heavy load. The circuit is implemented in a 2P4M 0.35μm CMOS process. A small external inductor of 0.47 μH and a capacitor of 4.7 μF are used to lower the cost of the converter and keep the output ripple to less than 10 mV. The measurement results show that the overshoot of the load transient response is 8 mV @ 200 mA step and the dynamic voltage scaling (DVS) performance is a rise of 16/zs/V and a fall of 20 μs/V. With a SAPTS technique and PFM control, the efficiency is maintained at more than 81% for a load range of 20 to 1500 mA and the peak efficiency reaches 88.43%.展开更多
When the chaotic characteristics of manufacturing quality level are studied, it is not practical to use chaotic methods because of the low speed of calculating the correlation integral. The original algorithm used to ...When the chaotic characteristics of manufacturing quality level are studied, it is not practical to use chaotic methods because of the low speed of calculating the correlation integral. The original algorithm used to calculate the correlation integral is studied after a computer hardware upgrade. The result is that calculation of the correlation integral can be sped up only by improving the algorithm. This is accomplished by changing the original algorithm in which a single distance threshold-related correlation integral is obtained from one traversal of all distances between different vectors to a high-efficiency algorithm in which all of the distance threshold-related correlation integrals are obtained from one traversal of all of the distances between different vectors. For a time series with 3000 data points, this high-efficiency algorithm offers a 3.7-fold increase in speed over the original algorithm. Further study of the high-efficiency algorithm leads to the development of a super-high-efficiency algorithm, which is accomplished by changing the original and high-efficiency algorithms, in which the add-one operation of the Heaviside function is executed n times, such that the execution of the add-one operation occurs only once. The super-high-efficiency algorithm results in increases in the calculation speed by up to 109 times compared with the high-efficiency algorithm and by approximately 404 times compared with the original algorithm. The calculation speed of the super-high-efficiency algorithm is suitable for practical use with the chaotic method.展开更多
文摘A current-mode buck DC-DC controller based on adaptive on-time (AOT) control is presented. The on-time is obtained by the techniques of input feedforward and output feedback, and the adaptive control is achieved by a sample-hold and time-ahead circuit. The AOT current-mode control scheme not only obtains excellent transient response speed, but also achieves the independence of loop stability on output capacitor ESR. In addition, the AOT current-mode control does not have subharmonic oscillation phenomenon seen in fixed frequency peak current-mode control, so there is no need of the slope compensation circuit. The auto-skip pulse frequency modulation (PFM) mode improves the conversion efficiency of light load effectively. The controller has been fabricated with UMC 0.6-μm BCD process successfully and the detailed experimental results are shown.
文摘A 1500 mA,10 MHz self-adaptive on-time (SOT) controlled buck DC-DC converter is presented. Both a low-cost ripple compensation scheme (RCS) and a self-adaptive on-time generator (SAOTG) are proposed to solve the system stability and frequency variation problem. Meanwhile a self-adaptive power transistor sizing (SAPTS) technique is used to optimize the efficiency especially with a heavy load. The circuit is implemented in a 2P4M 0.35μm CMOS process. A small external inductor of 0.47 μH and a capacitor of 4.7 μF are used to lower the cost of the converter and keep the output ripple to less than 10 mV. The measurement results show that the overshoot of the load transient response is 8 mV @ 200 mA step and the dynamic voltage scaling (DVS) performance is a rise of 16/zs/V and a fall of 20 μs/V. With a SAPTS technique and PFM control, the efficiency is maintained at more than 81% for a load range of 20 to 1500 mA and the peak efficiency reaches 88.43%.
文摘When the chaotic characteristics of manufacturing quality level are studied, it is not practical to use chaotic methods because of the low speed of calculating the correlation integral. The original algorithm used to calculate the correlation integral is studied after a computer hardware upgrade. The result is that calculation of the correlation integral can be sped up only by improving the algorithm. This is accomplished by changing the original algorithm in which a single distance threshold-related correlation integral is obtained from one traversal of all distances between different vectors to a high-efficiency algorithm in which all of the distance threshold-related correlation integrals are obtained from one traversal of all of the distances between different vectors. For a time series with 3000 data points, this high-efficiency algorithm offers a 3.7-fold increase in speed over the original algorithm. Further study of the high-efficiency algorithm leads to the development of a super-high-efficiency algorithm, which is accomplished by changing the original and high-efficiency algorithms, in which the add-one operation of the Heaviside function is executed n times, such that the execution of the add-one operation occurs only once. The super-high-efficiency algorithm results in increases in the calculation speed by up to 109 times compared with the high-efficiency algorithm and by approximately 404 times compared with the original algorithm. The calculation speed of the super-high-efficiency algorithm is suitable for practical use with the chaotic method.